Showing posts with label boost. Show all posts
Showing posts with label boost. Show all posts

Saturday, February 14, 2015

shakedown pulls tonight

did some quick shakedowns tonight, tires rubbing really badly front and back (front only when turning) and rear only on the outside, so i am gunna get these fenders rolled and pulled to clear, because i want to fit these 28s for best mph with my 355 gears, built in boost control in MS3 is flat out retardedly awesome, i told it what boost i wanted, and it was able to deliver easily, climbs to target and holds, didnt even get to mess with the sensitivity settings but i could make it target faster, made 2 dyno pulls, tires were rubbing so bad it made me nervous so i quit before i blew one of them off the car at 140 lol, car made 509whp on 13psi 10.40 AFR and 554whp on 14psi, hp still climbing great when i lifted nervously at 6400 haha it seems like its making around 40whp per psi right now, wich would be awesome to stay on track for 700 tire wich is my goal, im sure tire rub is eating a little power too, but successful trip! some things to address but i drove to the dyno and slammed down 500+ twice and came home without an issue! video is coming






Thursday, February 5, 2015

boost noid, trans cooler, etc

ebay boost controller solenoid mounted and wired, plumbed, ebay trans cooler mounted, wired, working, tested temp switch with a heat gun lol, and mickey mouse club dash ready for the driveshaft (on its way)




Wednesday, February 26, 2014

both cars done as is, as of today

just some completed pics of the cars today for fun, as is! both running and driving and making boost!








Saturday, February 8, 2014

Monday, December 2, 2013

got everything done with the truck!
so i tested out the trans and converter and fuel pump etc, doing great.


Sunday, October 13, 2013

tuning on 18psi highway third gear pull

stock 99 4.8 (only valvesprings installed $50 dollar comp electronics)
stock ls1 intake, stock fuel rails, stock throttle, heads (untouched from the yard)
stock paper head gaskets, stock head bolts, stock rings, rod bolts, etc
18psi (on3 76mm turbo .96 AR) 2 inch home made hotside, 2.5 inch cold side
harbor freight compressor regulator boost controller

sumped stock tank, bosch 044 fuel pump, returnless rail with aeromotive regulator attached. 3/8ths push lock lines. wawa 92 octane pumpgas with methanol (prestone washer fluid approx 30-30% alc)
4l80e, fox 8.8 rear with 3.73 gears. 31 spline mosers.


Saturday, October 5, 2013

getting there! fairmont driving video updates

this is yesterdays video from the car, 10-12psi and rough tune
and here is today at 14psi
doing pretty good!
gotta make my shifts sooner, its laying over power wise at 6000 it feels like, and looks like

Thursday, October 3, 2013

valvesprings and pressing on

installed the 50 dollar valve springs today to see how they do in comparison to the pac1218s wich are 140 ish... they seem good so far, i raised my boost to 10lbs without a problem right now, just crushed in some more wastegate spring for the car to see how it will do should be 14lbs of boost on the wastegate right now after this, probably going to add the methanol kit to the car tomorrow and continue pushing, also i think we are going to race the firebird tomorrow



Thursday, February 14, 2013

valentines day gift for the truck 12psi

so its been doing really well, time to up the boost, since it makes 4psi you can assume connecting top and bottom will make 2x the boost 8 psi, and disconnecting the wastegate entirely will make 12psi.

so i totally disconnected the WG and it makes 12psi!

it also frys the tires from a 2nd gear roll.


Friday, April 13, 2012

methanol installed, and boost controller for the 4.8 notch

installed a methanol kit today and the ebay boost controller with great sucess, the boost controller definately brought down the spool time by being a ball and spring and blocking reference for a few psi, and the meth kit held the car together when we learned we were out of fuel pump at 20+lbs of boost... LOL

it has a walboro 340lph stealth in the tank and well i can guarantee we are over 600rwhp because its smoking these 28x10.5 slicks from a 70 roll like they are shit.

15* 21lbs of boost, woot woot.

adding the 044 from the ventura tomorrow to see if we can remedy that then buying another 044 for the ventura... hopefully racing this 4.8 beast sunday.